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Abstract:
尤溪汶潭水利枢纽工程坝址上游为一个大弯道,主流偏向右岸(凹岸).该文通过整体水工模型试验,修改优化原设计方案电站取水口拦污栅结构和平面布置不合理处.试验结果表明:拦污栅结构和平面布置优化后,可以有效改善水闸泄洪流态和泄流能力.
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水利科技
ISSN: 1002-3011
CN: 35-1123/TV
Year: 2016
Issue: 4
Page: 59-61
Cited Count:
SCOPUS Cited Count:
ESI Highly Cited Papers on the List: 0 Unfold All
WanFang Cited Count: -1
Chinese Cited Count:
30 Days PV: 1
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